Another Day In The Life Of A
Gunsmith.
Wednesday, March 03, 2010 Filed in:
Gunsmithing, My
Life
Many people tell me that they'd love to have my job: "it must be
fun to play with all those cool guns and get paid for it!"
Lest others be deluded into thinking that this business is all fun
and games, allow me to supply a dose of reality: somedays it
literally doesn't pay to get out of bed.
Last Thursday was just such a day. It started with the need to make
a 'spud'. No, not a potato - a 'spud' is a metal pilot that aligns
a cutter with a bore. They're used as guides for such things as
chamfering chambers and crowning barrels.
You can buy them ready made, but they come in one size per
caliber-specific application. The problem is that if the spud is
even .001" off, the quality of the cut will be destroyed. They need
to be fitted precisely to the hole in which they will be inserted,
and the ready made variety never are. If good work is to be done,
they have to be custom made to fit the work.
Over the years I've made a wide range of spuds in various sizes,
and because of that selection I usually have one that will fit
properly. Occasionally, though, I run into a situation where I need
to make yet another one, which is what happened on Thursday. I
needed a .216" spud, and the closest I had was .214" - not nearly
good enough to properly crown the .22LR barrel on which I was
working.
Not a problem! I picked out some appropriate metal and chucked it
in the lathe. I made a couple of cuts to get close to finished
size, but when I measured the diameter I found that it tapered by
roughly .002" throughout the length of the piece! The spud is only
a couple of inches long, so a .002" variance in that length
is
huge. It renders the part
unusable.
It's also not supposed to happen.
Annoying, but not insurmountable. I thought that the lathe probably
just needed to be re-leveled, which hadn’t been done for a
couple of years. I leveled the lathe (which takes a couple of hours
if done very carefully), made a test cut, and....it was still
off!
Grrrrrr.
The next step was to check the lathe’s
tailstock for alignment. The
tailstock, which supports the end of work in a lathe, has to be
precisely aligned along the lathe's longitudinal axis. Otherwise,
it pulls the end of the piece left or right, which leads to a taper
such as I was finding. I spent the time aligning the tailstock, and
a quote from the movie "Ruthless People" poured from my mouth: "Now
THAT oughtta do it!"
It didn't.
I went back, tweaked the lathe level, and aligned the tailstock
again. The problem persisted.
Put yourself in my place: I've got a top-notch Austrian lathe, the
best Swiss measuring instruments, and I'm making parts displaying
precision more appropriate to a Kalashnikov clone produced in an
unlit cave factory outside of Jalalabad. Something was wrong, and I
had to find it. The only hitch was that it was now dinnertime, and
due to skipping lunch I was as hungry as could be. The problem
would have to wait until the next day.
Friday morning I came into work determined to find the cause.
Double checking everything revealed no clues. I replayed the issues
in my head, while at the same time resting my hand on the
tailstock. I looked down, and it came to me: the live center in the
tailstock must be the source of the problem. It was the only thing
I'd not checked.
A live center looks like this:

The cone-shaped bit is inserted into a hole in the piece being
machined, and the other end goes into the tailstock. The cone
revolves on precision ball bearings, keeping the piece aligned as
it's rotated by the lathe. Any rotational error will result in
inconsistencies in the finished part.
A quick check with a quality (Swiss) test indicator confirmed my
fears: .0025" wobble. I checked the piece I'd machined, in several
orientations, and sure enough - not only was it tapered, it was
also slightly oval, which is exactly the error a worn live center
would produce. Bingo!
I ordered up a new live center from my favorite online tool
supplier (www.mscdirect.com), and on Monday the smiling
UPS man delivered it to my door. The center quickly proved to be
the answer; the rotational error was less than .0001", compared to
the .0025" wobble of the old one.
With the new center a perfect spud was easily produced, the barrel
was beautifully crowned, and the gun will soon be on its way back
to a happy shooter.
It only took me a day and a half, plus a not insignificant amount
of cash to find and fix the problem. So, want to tell me again how
you wish you had my job?
-=[
Grant ]=-
Tags: dammit